Code | Cause | Remedy |
---|---|---|
E000 | Fixing temperature abnormal rise | |
0001 | The temperature detected by the main thermistor does not rise to the specified value during startup control. |
1. Go through the following to clear the error: CLEAR > ENGIN > ERRCLR; and then turn OFF and then ON the power. 2. Check connection of the Connectors (Thermistor Connector and AC Connector). 3. Replace the Fixing Main Thermistor (Film Unit). 4. Replace the Fixing Assembly. 5. Replace the DC Controller PCB (PCB4). |
E001 | Fixing unit temperature rise detection | |
0000 | The reading of the main thermistor is 250 deg C or more continuously for 200 msec. | 1. Go through the following to clear the error: CLEAR > ENGIN > ERRCLR; and then turn OFF and then ON the power. 2. Check connection of the Connectors (Thermistor Connector and AC Connector). 3. Replace the Fixing Main Thermistor (Film Unit). 4. Replace the Fixing Assembly. 5. Replace the DC Controller PCB (PCB4). |
0001 | The hardware circuit detects overheating of the main or sub thermistor for 200 msec. | 1. Go through the following to clear the error: CLEAR > ENGIN > ERRCLR; and then turn OFF and then ON the power. 2. Replace the DC Controller PCB (PCB4). |
0002 | The reading of the sub thermistor is 295 deg C or more continuously for 200 msec. | 1. Go through the following to clear the error: CLEAR > ENGIN > ERRCLR; and then turn OFF and then ON the power. 2. Check connection of the Connectors (Thermistor Connector and AC Connector). 3. Replace the Fixing Main Thermistor (Film Unit). 4. Replace the Fixing Assembly. 5. Replace the DC Controller PCB (PCB4). |
E002 | Fixing unit temperature insufficient rise | |
0000 | 1. The reading of the main thermistor is less than 115 deg C continuously for 400 msec 1.3 sec after it has indicated 100 deg C. 2. The reading of the main thermistor is less than 150 deg C continuously for 400 msec 1.3 sec after it has indicated 140 deg C. |
1. Go through the following to clear the error: CLEAR > ENGIN > ERRCLR; and then turn OFF and then ON the power. 2. Check connection of the Connectors (Thermistor Connector and AC Connector). 3. Replace the Fixing Main Thermistor (Film Unit). 4. Replace the Fixing Assembly. 5. Replace the DC Controller PCB (PCB4). |
E003 | Low fixing temperature detection after standby | |
0000 | The reading of the main thermistor is less than 140 deg C continuously for 400 msec or more. | 1. Go through the following to clear the error: CLEAR > ENGIN > ERRCLR; and then turn OFF and then ON the power. 2. Check connection of the Connectors (Thermistor Connector and AC Connector). 3. Replace the Fixing Main Thermistor (Film Unit). 4. Replace the Fixing Assembly. 5. Replace the DC Controller PCB (PCB4). |
E004 | Thermistor disconnection detection error | |
0000 | When disconnection is detected with connector (J214) for 30 sec continuously. | 1. Check connection of the Connector (J214). 2. Replace the Film Unit. 3. Replace the Fixing Assembly. 4. Replace the DC Controller PCB (PCB4). |
E010 | Unstable rotation of the Main Motor (M1) | |
0001 | Detection is executed every 100 msec after the start of motor rotation; however, the drive detection signal is absent for 2 sec. | 1. Replace the Main Motor (M1). 2. Replace the DC Controller PCB (PCB4). |
0002 | During motor rotation, detection is executed every 100 msec; however, the drive signal is absent 5 times in sequence. | |
E014 | Unstable rotation of the Fixing Motor (M2) | |
0001 | Detection is executed every 100 msec after the start of motor rotation; however, the drive detection signal is absent for 2 sec. | 1. Replace the Fixing Motor (M2). 2. Replace the DC Controller PCB (PCB4). |
0002 | During motor rotation, detection is executed every 100 msec; however, the drive signal is absent 5 times in sequence. | |
E019 | Error in Waste Toner Sensor (S17) | |
0000 | Warning when the sensor goes on for 2000 consecutive sheets, and error when the sensor goes on for 100 consecutive sheets. * Error occurs after the delivery if a paper in passage exists. |
1. Replace the Waste Toner Sensor (S17). 2. Replace the DC Controller PCB (PCB4). |
E020 | The path between the sub hopper and the developing assembly is clogged with toner. | |
0000 | The Developing Assembly Toner Sensor (TS1) detects the absence of
toner,while the Sub Hopper Toner Sensor (TS2) detects the presence of
toner. With the Developing Cylinder Clutch (CL3) turned on, the hopper
feedscrew motor (M7) is rotated for 1 sec intermittently 194 times;
still, theDeveloping Assembly Toner Sensor (TS1) does not detect the
presence of toner. * Error occurs after the delivery if a paper in passage exists. |
1. Check the rotation of hopper motor gear. (If rotating, false
detection by the sensor is doubted. Feed the toner to the developing
unit in service mode: CLEAR>ENGIN>TNRINST.) 2. Replace the Developing Assembly Toner Sensor (TS1). 3. Replace the Sub Hopper Toner Sensor (TS2). 4. Replace the DC Controller PCB (PCB4). |
E024 | Developing Assembly Toner Sensor (TS1) is disconnected. | |
0000 | The Developing Assembly Toner Sensor (TS1) connection detection signal is absent for 100 msec 10 times in sequence. * Error occurs after the delivery if a paper in passage exists. |
1. Check connection of the Connector (J207). 2. Replace the Developing Assembly Toner Sensor (TS1). 3. Replace the DC Controller PCB (PCB4). |
0001 | <At LOW SPEED> The developing assembly toner sensor (TS1) ON counter is checked every 2.5 seconds, and the counter increments 1 count every 25 times when the sensor goes on, and 300 counts are reached. <At HIGH SPEED> The developing assembly toner sensor (TS1) ON counter is checked every 1.5 seconds, and the counter increments 1 count every 15 times when the sensor goes on, and 300 counts are reached. |
1. Check connection of the Connector (J207). 2. Correct the cable. 3. Replace the Developing Assembly Toner Sensor (TS1). |
E025* | The connector (J207) of Sub Hopper Toner Sensor (TS2) is disconnected | |
0000 | The Sub Hopper Toner Sensor (TS2) connection detection signal is absent for 100 msec 10 times in sequence. * Error occurs after the delivery if a paper in passage exists. |
1. Check connection of the Connector (J207). 2. Replace the Sub Hopper Toner Sensor (TS2). 3. Replace the DC Controller PCB (PCB4). |
E025* | Failure of the Bottle Motor (M6) | |
0001 | The bottle motor (M6) is unlocked when it goes on for 12 consecutive times at 0.1 sec. intervals. * Error occurs after the delivery if a paper in passage exists. |
1. Replace the Bottle Motor (M6). 2. Replace the DC Controller PCB (PCB4). |
E110 | Failure of the Scanner Motor (M21) | |
0001 | The Scanner Motor (M21) speed lock signal does not indicate a
locked state a specific period of time after the Scanner Motor (M21) has
been started. * The same condition is detected after the error retry is performed. |
1. Check the cable. 2. Replace the Laser Scanner Unit. 3. Replace the DC Controller PCB (PCB4). |
0002 | The speed lock signal indicates a deviation 10 times in sequence
at intervals of 100 msec after the signal has indicated a locked state. * The same condition is detected after the error retry is performed. | |
0003 | The scanner motor (M21) speed lock signal does not indicate a
locked state for 6.5 sec. after a switchover is made from low to normal
speed or for 8 sec. after a switchover is made from normal to low speed. * The same condition is detected after the error retry is performed. | |
E196 | Error in EEPROM access | |
0000 | 20 retries failed after error occurred during communication with EEPROM. * Error occurs after the delivery if a paper in passage exists. |
Replace the DC Controller PCB (PCB4). |
E197 | Error in communication of Laser Driver PCB (PCB14) | |
0000 | Communication error 1 with image PCB | 1. Check the cable. 2. Replace the Laser Scanner Unit. 3. Replace the DC Controller PCB (PCB4). |
0001 | Communication error 2 with image PCB | |
E202 | There is an error in the detection of the CIS home position. | |
0000 | 1. The attempt to detect the home position fails when the CIS is moved forward. 2. The attempt to detect the home position fails when the CIS is moved back. |
1. Disconnect and then connect the flexible cable(Relay PCB (PCB2)-Main Controller PCB (PCB1) 64pin). 2. Replace the flexible cable. 3. Replace the CIS HP sensor (S31). 4. Replace the Scanner Motor (M31). 5. Replace the Relay PCB (PCB2). 6. Replace the Main Controller PCB (PCB1). |
E225 | The light intensity of the CCD is faulty. | |
0000 | The light intensity of the CCD during shading is under the specified level. | 1. Disconnect and then connect the flexible cable. 2. Replace the flexible cable. 3. Replace the CCD Unit. 4. Replace the Relay PCB (PCB2). 5. Replace the Main Controller PCB (PCB1). |
E227 | The reader unit power supply (24V) is faulty. | |
0000 | 1. At time of power-on, the 24V port is off. 2. At the start of a job, the 24V port is off. 3. At the end of a job, the 24V port is off. 4. When a load is being driven, the 24V port is off. |
1. Disconnect and then connect the power supply harness connector. 2. Replace the Power Supply PCB (PCB3). |
E240 | Error in controller communication | |
0000 | The serial communication error such as parity error or overrun error is constantly detected. | 1. Check the Connectors. 2. Replace the DC Controller PCB (PCB4). |
0001 | The serial communication error such as parity error or overrun error is detected while printing. | |
E248 | EEPROM error | |
0000 | 1. An error has occurred at power-on. 2. An error has occurred during write operation. 3. An error has occurred during read operation following write operation. |
1. Disconnect and then connect the flexible cable(Relay PCB (PCB2)-Main Controller PCB (PCB1) 50pin). 2. Disconnect and then connect the flexible cable(CCD unit-Relay PCB (PCB2)). 3. Disconnect and then connect the power supply harness connector. 4. Replace the flexible cable. 5. Replace the CCD Unit. 6. Replace the Relay PCB (PCB2). 7. Replace the Power Supply PCB (PCB3). 8. Replace the Main Controller PCB (PCB1). |
E261 | Error in Zero Cross | |
0000 | Zero Cross failed to be detected for 500ms or more while the relay was ON. * The same condition is detected after the error retry is performed. |
1. Check the Connectors. 2. Replace the DC Controller PCB (PCB4). |
E280 | Reading unit communication error | |
0000 | Reading error after writing. | 1. Disconnect and then connect the flexible cable(Relay PCB (PCB2)-Main Controller PCB (PCB1) 50pin). 2. Disconnect and then connect the flexible cable(Relay PCB (PCB2)-Main Controller PCB (PCB1) 64pin). 3. Disconnect and then connect the flexible cable(CCD unit-Relay PCB (PCB2)). 4. Replace the flexible cable. 5. Replace the Relay PCB (PCB2). 6. Replace the Main Controller PCB (PCB1). |
E413 | Release Motor (M2) error | |
0000 | The sensing level of the release motor HP sensor (SR11) does not change within a specified period when the release motor (M2) is driven. | 1. Replace the Release Motor HP Sensor (SR11). 2. Replace the Release Motor (M2). 3. Replace the ADF Driver PCB. |
E500 | Communication error | |
0000 | The communication with the host machine is interrupted. | 1. Check the cable. 2. Replace the Finisher Controller PCB (PCB1). 3. Replace the DC Controller PCB. |
E505 | EEPROM error | |
0001 | The checksum for the EEPROM data has an error. | Replace the Finisher Controller PCB (PCB1). |
E520 | Shift Motor (M4) error | |
0001 | The shift roller does not leave the shift roller home position when the Shift Motor (M4) has been driven for 1.2 seconds. | 1. Replace the Shift Roller HP Sensor (S2). 2. Replace the Shift Motor (M4). 3. Replace the Finisher Controller PCB (PCB1). |
0002 | The shift roller does not return to the shift roller home position when the Shift Motor (M4) has been driven for 1.2 seconds. | |
E531 | Stapler Motor (M10) error | |
8001 | The stapler does not leave the staple home position when the Staple Motor (M10) has been driven for 0.5 sec. | 1. Check the wiring between the Finisher Controller PCB and Stapler. 2. Replace the Stapler. 3. Replace the Finisher Controller PCB (PCB1). |
8002 | The stapler does not return to the staple home position when the Stapler Motor (M10) has been driven for 0.5 sec. | |
E532 | STP Move Motor (M1) error | |
0001 | The stapler does not leave the stapler move home position when the STP Move Motor (M1) has been driven for 0.25 sec. | 1. Replace the Stapler Move HP Sensor (S10). 2. Check the wiring between the Finisher Controller PCB and the STP Move Motor. 3. Check the stapler shift base. 4. Replace the STP Move Motor (M1). 5. Replace the Finisher Controller PCB (PCB1). |
0002 | The stapler does not return to the stapler move home position when the STP Move Motor (M1) has been driven for 2.8 sec. | |
E540* | Tray Lift Motor (M11) time out error | |
0001 | The stack tray does not move within a specified time period. | 1. Replace the Tray Lift Motor (M11). 2. Replace the Finisher Controller PCB (PCB1). |
E540* | Tray Lift Motor (M11) closing detect switch error | |
0005 | The FG input cannot be detected when the Tray Lift Motor (M11) has been driven for 0.1 second. | 1. Replace the Stack Tray Clock Sensor (S13). 2. Replace the Tray Lift Motor (M11). 3. Replace the Finisher Controller PCB (PCB1). |
E542* | Additional Tray Lift Motor (M12) time out error | |
0001 | The stack tray does not move within a specified time period. | 1. Replace the Additional Tray Lift Motor (M12). 2. Replace the Finisher Controller PCB (PCB1). |
E542* | Additional Tray Lift Motor (M12) closing detect switch error | |
0005 | The FG input cannot be detected when the Additional Tray Lift Motor (M12) has been driven for 0.1 second. | 1. Replace the Additional Tray Clock Sensor (S23). 2. Replace the Additional Tray Lift Motor (M12). 3. Replace the Finisher Controller PCB (PCB1). |
E567 | Shift Roller Release Motor (M5) error | |
0001 | The shift roller does not leave the shift roller release home position when the Shift Roller Release Motor (M5) has been driven for 0.1 sec. | 1. Replace the Shift Roller Release Sensor (S3). 2. Replace the Shift Roller Release Motor (M5). 3. Replace the Finisher Controller PCB (PCB1). |
0002 | The shift roller does not return to the shift roller release home position when the Shift Roller Release Motor (M5) has been driven for 0.06 sec. | |
E571 | Gripper Open/Close Motor (M7) error | |
0001 | The gripper unit does not leave the gripper unit home position when the Gripper Open/Close Motor (M7) has been driven for 0.25 seconds. | 1. Replace the Grip Arm Sensor (S13). 2. Replace the Gripper Open/Close Motor (M7). 3. Replace the Finisher Controller PCB (PCB1). |
0002 | The gripper unit does not return to the gripper unit home position when the Gripper Open/Close Motor (M7) has been driven for 0.15 seconds. | |
E575 | Gripper Unit Move Motor (M2) error | |
0001 | The gripper unit does not leave the gripper unit home position when the Gripper Unit Move Motor (M2) has been driven for 3.8 seconds. | 1. Replace the Gripper Unit HP Sensor (S7). 2. Replace the Gripper Unit Move Motor (M2). 3. Replace the Finisher Controller PCB (PCB1). |
0002 | The gripper unit does not return to the gripper unit home position when the Gripper Unit Move Motor (M2) has been driven for 0.1 seconds. | |
E602 | The built-in SD card is not detected | |
0001 | — | — |
E602 | Access to the built-in SD card failed | |
1105 | — | — |
E711 | Error in UFDI communication | |
0001 | The communication system error (such as reception timeout or checksum error) occurred. | 1. Check and Replace the cable. 2. Replace the DC Controller PCB (PCB4). 3. Replace the Finisher Controller PCB. |
E713 | Erroneous communication with finisher | |
0000 | The communication does not restart by the error retry after the communication failure with the finisher. | 1. Check the cable. 2. Replace the DC Controller PCB (PCB4). 3. Replace the Finisher Controller PCB. |
E716 | Erroneous communication with optional cassette or 2-way unit | |
0000 | After the presence of a cassette pedestal or a 2-way unit has been detected, the communication fails to be normal for 5 sec. | 1. Check the cable. 2. Replace the DC Controller PCB (PCB4). 3. Replace the Cassette Pedestal Driver PCB. 4. Replace the 2-way unit driver PCB. |
0010 | When the communication with the 2-way unit is faulty after detecting the connection with the finisher. | 1. Install the 2-way unit. 2. Check the cable. 3. Replace the DC Controller PCB (PCB4). 4. Replace the 2-way unit driver PCB. |
E719 | Erroneous communication with New Card Reader (serial communication) | |
0000 | — | — |
E719 | Erroneous communication with Coin Vendor (serial communication) | |
0002 | — | — |
E736 | Erroneous communication between CCU and controller. | |
0000 | — | — |
E744 | Mismatched version between the language file and the Bootable | |
0001 | — | — |
0003 | — | — |
E744 | Oversized language file in HDD | |
0002 | — | — |
E744 | Language file reading error | |
0004 | — | — |
E804 | Failure of the Power Supply Cooloing Fan (FAN6) | |
0000 | When lock signal is detected for 5 sec while the Power Supply Cooloing Fan (FAN6) is stopped. * The same condition is detected after the error retry is performed. |
1. Disconnect and then connect the connector (J205) on the DC Controller PCB (PCB4). 2. Replace the Power Supply Cooloing Fan (FAN6). 3. Replace the DC Controller PCB (PCB4). |
0001 | When lock signal failed to be detected for 5 sec while the Power Supply Cooloing Fan (FAN6) is driven. * The same condition is detected after the error retry is performed. | |
E805* | Failure of the Exhaust Fan (Rear) (FAN3) | |
0000 | When lock signal is detected for 5 sec while the Exhaust Fan (Rear) (FAN3) is stopped. * The same condition is detected after the error retry is performed. |
1. Disconnect and then connect the connector (J206) on the DC Controller PCB (PCB4). 2. Replace the Exhaust Fan (Rear) (FAN3). 3. Replace the DC Controller PCB (PCB4). |
E805* | Unstable rotation of the Exhaust Fan (Rear) (FAN3) or Finisher Fan 1 (M8) or Finisher Fan 2 (M9) | |
0001 | 1. When lock signal failed to be detected for 5 sec while the Exhaust Fan (Rear) (FAN3) is driven. 2. When lock signal failed to be detected for 5 sec while the Finisher Fan 1 (M8) is driven. 3. When lock signal failed to be detected for 5 sec while the Finisher Fan 2 (M9) is driven. * The same condition is detected after the error retry is performed. |
1. Disconnect and then connect the connector (J206) on the DC Controller PCB (PCB4). 2. Replace the Exhaust Fan (Rear) (FAN3). 3. Replace the Finisher Fan 1 (M8). 4. Replace the Finisher Fan 2 (M9). 5. Replace the DC Controller PCB (PCB4). |
E805* | Failure of the Exhaust Fan (Front) (FAN4) | |
0002 | When lock signal is detected for 5 sec while the Exhaust Fan (Front) (FAN4) is stopped. * The same condition is detected after the error retry is performed. |
1. Disconnect and then connect the connector (J206) on the DC Controller PCB (PCB4). 2. Replace the Exhaust Fan (Front) (FAN4). 3. Replace the DC Controller PCB (PCB4). |
0003 | When lock signal failed to be detected for 5 sec while the Exhaust Fan (Front) (FAN4) is driven. * The same condition is detected after the error retry is performed. |
Сервисные коды ошибок факса
Code | Tx/Rx | Description |
---|---|---|
##0100 | Tx | At time of transmission, the procedural signal has been transmitted more than specified. |
##0101 | Tx/Rx | The modem speed does not match that of the other party. |
##0102 | Tx | At time of transmission, fall-back cannot be used. |
##0103 | Rx | At time of reception, EOL cannot be detected for 5 sec (15 sec if CBT). |
##0104 | Tx | At time of transmission, RTN or PIN is received. |
##0106 | Rx | At time of reception, the procedural signal is received for 6 sec while in wait for the signal. |
##0107 | Rx | At time of reception, the transmitting party cannot use fall-back. |
##0109 | Tx | At time of transmission, a signal other than DIS, DTC, FTT, CFR, or CRP is received, and the procedural signal has been sent more than specified. |
##0111 | Tx/Rx | Memory error has occurred |
##0114 | Rx | At time of reception, RTN is transmitted. |
##0200 | Rx | At time of reception, no image carrier is detected for 5 sec. |
##0201 | Tx/Rx | DCN is received outside the normal parity procedure. |
##0224 | Tx | Communication protocol signal error. |
##0228 | Rx | Abnormal management information of image data |
##0232 | Tx | Encoding error has occurred. |
##0237 | Rx | Decoding error has occurred. |
##0261 | Tx/Rx | System error has occurred. |
##0280 | Tx | At time of transmission, the procedural signal has been transmitted more than specified. |
##0281 | Tx | At time of transmission, the procedural signal has been transmitted more than specified. |
##0282 | Tx | At time of transmission, the procedural signal has been transmitted more than specified. |
##0283 | Tx | At time of transmission, the procedural signal has been transmitted more than specified. |
##0284 | Tx | At time of transmission, DCN is received after transmission of TCF. |
##0285 | Tx | At time of transmission, DCN is received after transmission of EOP. |
##0286 | Tx | At time of transmission, DCN is received after transmission of EOM. |
##0287 | Tx | At time of transmission, DCN is received after transmission of MPS. |
##0288 | Tx | After transmission of EOP, a signal other than PIN, PIP, MCF, RTP, or RTN has been received. |
##0289 | Tx | After transmission of EOM, a signal other than PIN, PIP, MCF, RTP, or RTN has been received. |
##0290 | Tx | After transmission of MPS, a signal other than PIN, PIP, MCF, RTP, or RTN has been received. |
##0670 | Tx | At time of V.8 lAte start, the V.8 ability of DIS front the receiving party is expected to be detected, and the CI signal is expected to be transmitted in response; however, the procedure fails to advance, and the line is released because of T1 time-out. |
##0671 | Rx | At time of V.8 arrival, procedure fails to move to phase 2 after detection of CM signal from caller, causing T1 time-out and releasing line. |
##0672 | Tx | At time of V.34 transmission, a shift in procedure from phase 2 to phase 3 and the reafter stops, causing the machine to release the line and suffer T1 timeout. |
##0673 | Rx | At time of V.34 reception, a shift in procedure from phase 2 to phase 3 and thereafter stops, causing the machine to release the line and suffer T1 timeout. |
##0674 | Tx | At time of V.34 transmission, a shift in procedure from phase 3 and phase 4 to the control channel and thereafter stops, causing the machine to release the line and suffer T1 timeout. |
##0675 | Rx | At time of V.34 reception, a shift in procedure from phase 3 and phase 4 to the control channel and thereafter stops, causing the machine to release the line and suffer T1 timeout. |
##0750 | Tx | At time of ECM transmission, no meaningful signal is received after transmission of PPS-NULL, causing the procedural signal to be transmitted more than specified. |
##0752 | Tx | At time of ECM transmission, DCN is received after transmission of PPS-NULL. |
##0753 | Tx | At time of ECM transmission, the procedural signal has been transmitted more than specified after transmission of PPS-NULL, or T5 time-out (60 sec) has occurred. |
##0754 | Tx | At time of ECM transmission, the procedural signal has been transmitted more than specified after transmission of PPS-NULL. |
##0755 | Tx | At time of ECM transmission, no meaningful signal is received after transmission of PPS-MPS, causing the procedural signal to be transmitted more than specified. |
##0757 | Tx | At time of ECM transmission, DCN is received after retransmission of PPS-MPS. |
##0758 | Tx | At time of ECM transmission, the procedural signal has been transmitted more than specified after transmission of PPS-MPS, or T5 time-out (60 sec) has occurred. |
##0759 | Tx | At time of ECM transmission, the procedural signal has been transmitted more than specified after transmission of PPS-MPS. |
##0762 | Tx | At time of ECM transmission, DCN is received after transmission of PPS-EOM. |
##0763 | Tx | At time of ECM transmission, the procedural signal has been transmitted more than specified after transmission of PPS-MPS, or T5 time-out (60 sec) has occurred. |
##0764 | Tx | At time of ECM transmission, the procedural signal has been transmitted more than specified after transmission of PPS-EOM. |
##0765 | Tx | At time of ECM transmission, no meaningful signal is received after transmission of PPS-EOP, causing the procedural signal to be transmitted more than specified. |
##0767 | Tx | At time of ECM transmission, DCN is received after transmission of PPS-EOP. |
##0768 | Tx | At time of ECM transmission, the procedural signal has been transmitted more than specified after transmission of PPS-EOP, or T5 time-out (60 sec) has occurred. |
##0769 | Tx | At time of ECM transmission, the procedural signal has been transmitted more than specified after transmission of PPS-EOP, or T5 time-out (60 sec) has occurred. |
##0770 | Tx | At time of ECM transmission, no meaningful signal is received after transmission of EOR-NULL, causing the procedural signal to be transmitted more than specified. |
##0772 | Tx | At time of ECM transmission, DCN is received after transmission of EOR-NULL. |
##0773 | Tx | At time of ECM transmission, the procedural signal has been transmitted more than specified after transmission of EOR-NULL, or T5 time-out (60 sec) has occurred. |
##0774 | Tx | At time of ECM transmission, ERR is received after transmission of EOR-NULL. |
##0775 | Tx | At time of ECM transmission, no meaningful signal is received after transmission of EOR-MPS, causing the procedural signal to be transmitted more than specified. |
##0778 | Tx | At time of ECM transmission, the procedural signal has been transmitted more than specified after transmission EOR-MPS, or T5 time-out (60 sec) has occurred. |
##0779 | Tx | At time of ECM transmission, ERR is received after transmission of EOR-MPS. |
##0780 | Tx | At time of ECM transmission, no meaningful signal is received after transmission of EOR-EOM, causing the procedural signal to be transmitted more than specified. |
##0782 | Tx | At time of ECM transmission, DCN is received after transmission of EOR-EOM. |
##0783 | Tx | At time of ECM transmission, the procedural signal has been transmitted more than specified after transmission of EOR-EOM, or T5 time-out (60 sec) has occurred. |
##0784 | Tx | At time of ECM transmission, no meaningful signal is received after transmission of EOR-EOP, causing the procedural signal to be transmitted more than specified. |
##0787 | Tx | At time of ECM transmission, DCN is received after transmission of EOR-EOP. |
##0788 | Tx | At time of ECM transmission, the procedural signal has been transmitted more than specified after transmission of EOR-EOP, or T5 time-out (60 sec) has occurred. |
##0789 | Tx | At time of ECM transmission, ERR is received after transmission of EOR-EOP. |
##0790 | Rx | At time of ECM reception, ERR is transmitted after transmission of EOR-Q. |
##0791 | Tx | While ECM mode procedure is under way, a signal other than a meaningful signal is received. |
##0792 | Rx | At time of ECM reception, PPS-NULL cannot be detected over partial page processing. |
##0793 | Rx | At time of ECM reception, no effective frame is received while high-speed signal reception is under way, thus causing time-out. |
##0794 | Tx | At time of ECM reception, PPR with all 0s is received. |
##0795 | Tx/Rx | A fault has occurred in code processing for communication. |